Cheers for all the help guys been working on the car today. got the problem sorted fingers crossed it stays that way.
started by taking the full airbox and all pipework off its shocking how bad them pipes were held together had about 1mm play. tapped the split hose up as a temporary measure but still got a good seal.
Took the sensor thing off and cleaned with carb cleaner blocked one end up filled up with cleaner and let soak for a hour.
Give all pipes a good clean took air box out the air filter was in a shocking state that hadn't been change in a while i wouldn't of said. it seems strange to spend all that money on the car and not change cheap service parts and that pipework setup was shocking. Just took air filter out new service kit is on order so car will be fully serviced soon as that lands.
Tried to run the normal fuel pressure reg if that's what its called disconnected the red one but once the car was all back together it wouldn't run. so had to connect the old one back up.
Car started great sounded nice on tick over went for a 20 min drive at all different types of driving pushed the car when i could after 10 min of normal driving without fault sound perfect no blips jumps or anything I am over the moon
Thanks again guys for all the help i have also found a guy local to me called big fish tuning have had a few cars tuned in the past basic maps on audi/vws tdi's. But he has a rolling road and would be good to listen to his input and see if the car is performing at its best.
Any help on a fuel regulator bmw part that would work that would bolt on so i could ditch that red thing would be a great help cheers
will order a leangh on 70mm samco house 6 inches long so it gets rid of that bodge pipe
