Woohoo. Finally made some good progress. fitted all the pipework and I/C and did some basic mapping. Managed a best run on the dyno of 209bhp @ 5800rpm.
It still needs some fettling for daily use though. Need to improve the bypass system and get more air over the I/C.
Dyno charts and pics will be posted soon.
-- update --
Finally got around to putting Megasquirt back on and fixed up some problems with it - pics and details on bottom of page 3.
Supercharger is bolted on and now the only real problem is getting the pipework sorted which should be easy.
-- update --
New dyno chart on page 2 - stock ecu and no supercharger. Finally it's making the correct power (143bhp) after the cam timing was sorted. Still no supercharger yet though.
-- update --
dyno chart lower down.
-- Update --
Well, I'm over 250 running in miles. A bit of oil dripping that I need to identify and it seems to use some water so I need to keep an eye on that. Hopefully neither are too serious and I'll be bolting the charger back on soon.
Still got to sort that saxo PS pump out as well.
I just have no time :'(
--Update--
Well.. After I don't know how much pissing about dan and I finally took her out for a spin. Put about 15-20 or so miles on I reckon, nothing above 3k for now. Here's a youtube video of her idling. The ticking is just the injectors, it's so quiet it makes them sound loud. Maybe that's normal but for me it's a novelty as now it's quieter both inside and outside, even without either the bonnet or gear-stick rubber seal. So nice.
In fairness I shouldn't get too excited. It's now time to get some miles on it, change the oil and flush the coolant etc then see if there's anything serious wrong.
Oh - I think it's time for a re-shell so if anybody knows a minter pls let me know
----
Hi all,
After fitting the supercharger that I've been working on for god knows how long, and making a bit of a bodge of it. I decided it was time to start doing things properly. First up was a complete engine rebuild. I used Dan318iS's old engine as well as some parts from my own. Last week we spent too many hours working on various things including the rebuild.
Still got a few more things to do before turning the key but it should be happening in the next few days.
I've got loads of pics to put up but he's one of my ugly mug trying to stick the engine back in it's rightful place.
Major thanks to Dan for his help with this!!!






































