Fuelling/electrics problem - any ideas appreciated
Posted: Fri Aug 09, 2013 9:49 am
Out for a drive one night the E30 just stopped running, in the middle of a roundabout. Electrics were on and engine would turnover but not fire.
After getting brought home on the back of a low loader I found that it was the fuel pump that had packed up, so I took the assembly out of the tank, swapped the pump, refitted and it ran OK again.
Briefly.
It fairly quickly developed an issue where it would drive OK 70% of the time and occasionally splutter/try to stop and then run OK again. Full details of this here, but it seemed like swapping the DME relay fixed the problem: http://www.e30zone.net/modules.php?name ... c&t=241413
Last night, out for a ride again, stopped at the Golden Arches for a milkshake, when I went to start the car it seemed like the fuel pump had gone (the brand new one) again. Turning over but not firing.
I tried short wiring the DME relay and replacing it for a spare I had with me, no joy. I've not yet had the fuel pump out and tested it independently but it certainly seems like it's gone pop (will test this weekend).
Do you know of anything that could cause this?
Any advice, suggestions or wild theories appreciated!
Cheers
After getting brought home on the back of a low loader I found that it was the fuel pump that had packed up, so I took the assembly out of the tank, swapped the pump, refitted and it ran OK again.
Briefly.
It fairly quickly developed an issue where it would drive OK 70% of the time and occasionally splutter/try to stop and then run OK again. Full details of this here, but it seemed like swapping the DME relay fixed the problem: http://www.e30zone.net/modules.php?name ... c&t=241413
Last night, out for a ride again, stopped at the Golden Arches for a milkshake, when I went to start the car it seemed like the fuel pump had gone (the brand new one) again. Turning over but not firing.
I tried short wiring the DME relay and replacing it for a spare I had with me, no joy. I've not yet had the fuel pump out and tested it independently but it certainly seems like it's gone pop (will test this weekend).
Do you know of anything that could cause this?
Any advice, suggestions or wild theories appreciated!
Cheers